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Gas Yamaha Gas Yamaha Golf Cars; G1 through "The Drive" and U-Max Utility Vehicles |
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#1 |
Not Yet Wild
Join Date: Apr 2008
Posts: 2
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![]() Hello guys I'm a newbie. I have a 82' G1 has the gov. an oil pump bypassed. It has power spring, 12 in Hazard wheel set, Grant GT steering wheel and new leather seat skins.
My problem is the cart doesn't wind all the way out. When it is jacked up, you can push the pedal down about half way and it seem to be fine but when you go from there to full throttle it sputers and won't wind out unless you pull the choke out then it winds all the way out . When driving it with a load on, it won't wind out even with the choke pulled out. I had a tech at buggies unlimited tell me that a ring may be bad if the compression is below 110lbs. Well I did a comp. test and it only hit 88-90lbs. It was just rebuilt last year and we bought it during the break in period. Would this be possibly why it can't wind out with a load on it? Could it not have been broke in properly? Sorry explaination is so long guys. |
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#2 | |
Sometime's............
![]() ![]() Join Date: Oct 2007
Location: Tacoma Washington
Posts: 11,806
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#3 |
Not Yet Wild
Join Date: Apr 2008
Posts: 2
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![]() I have the purchase order for a cylinder head kit which I asume is piston/ring/reed/gasket kit. Also the crank seals were replaced at the same time. I checked the fuel pressure and it is good so I'm pretty sure the seals are good. I think he did a quick rebuild and slaped everything together. I will go ahead and tear it down and check the rings piston and cylinder. Thanks. Shawn
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#4 |
Not Yet Wild
Join Date: Apr 2008
Posts: 2
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![]() I took the head off today and it looks to be in good shape. I wiped down and cleaned everything and put it back together because it seemed like the head bolts wern't very tight when I took it apart. The comp. went up to 95lbs. So I took it for a spin and it ran alot better and gained more speed an RPM. When I got back I did a comp. test and it went back down to 75-80lbs. Should I replace the head, reed, gaskets and crank seals? What about the lower cyl. gasket or is that unlikely?
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